33 Coupe Adjusting and Tweaking 14        5/16/09

 
This is what I came up with to get that seal out, a small slide hammer that I made. I welded a hex-key on one end and double-nutted the other to act as a stop. The round piece of steel which acts as my weight I made at work, which is 1 1/4" X 4" round stock with a 7/16" hole through it.

My plan was to have the end of the hex-key up against the back of the seal and then pound away on it till it came out. It sounded good to me but the only thing that happened was the front of the seal got deformed and pushed out. No matter how many times I tried, the end of the hex-key tried to slide off and ended up slipping more than anything else.

After working for about an hour with this tool, I gave up and went back to the drawing board in search of something else.
 

 

 

You know the ol' story, when in doubt use a bigger hammer, which is just what I did. Although this doesn't look like a hammer, you haven't seen the whole tool yet. Check out what I came up with to get that seal out.

Oh by the way, now you can see how the first tool deformed the face of the seal. This is what prompted me to try something else.
 

 

 

I made a slide hammer out of a pair of vise-grips. I thought that if I could bend the front lip of the seal out just a little with some pliers, then I could grab it with a something. Well the something that I came up with was a pair of vise-grips on steroids. The thread size of my vise-grips were 7/16" so all I needed was some all-thread that size and a larger piece of steel for the hammer part.

This time I used 1 3/4" diameter material for the hammer and once I tightened the vise-grips down, all it took was two or three whacks and out it came. That put a nice big smile on my face. And after I had everything all nice and clean, it was time to put the new seal in.
 

 

 

It sure is nice working at a machine shop because I can dream up things and make just about anything I want. This is what I made to press in the new seal. It's made out of aluminum and slips over the end of the crankshaft. The hole is 7/16" diameter which is the same size as the harmonic damper bolt. And the front lip of the tool is the same as the seal face so it shouldn't hurt it as I press it in.
 

 

 

Here you can see the new tool in action. I used a few washers to take up the extra length of the damper bolt and after a little black RTV on the outside of the seal, it went right in. This worked really well and I know it went in nice and straight too. One more thing, I didn't even have to swing a hammer to install it either.

It's been about three weeks now and there hasn't been any leaks so everything is working great again. And while I had the radiator out along with a few other items, I was able to get at some of the hard to reach areas and cleaned things up a little. I'm glad it only ended up being the timing cover seal instead of the pan gasket because I didn't feel like messing with that. Although I didn't feel like messing with either one, I'd take the timing cover over the oil pan.

Let's hope I don't have to make any new tools for awhile because that might mean I'm having trouble again...and nobody wants to have that!!
 

 

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